Deepwater Horizon Spill Report Blames BP, Contractors, Government

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Deepwater Horizon Spill Report Blames BP, Contractors, Government

WASHINGTON, DC, November 17, 2010 (ENS) – Lack of a systematic approach to well safety, numerous flawed decisions, plus technical and operational breakdowns all contributed to the Deepwater Horizon oil rig explosion and massive spill from BP’s Macondo well in the Gulf of Mexico, says a scientific committee of the National Academy of Engineering and National Research Council in a report released today.

“Important decisions made to proceed toward well abandonment despite several indications of potential hazard suggest an insufficient consideration of risks,” said Donald Winter, former secretary of the Navy, professor of engineering practice at the University of Michigan, and chair of the 15-member study committee.

“It’s also important to note that these flawed decisions were not identified or corrected by BP and its service contractors, or by the oversight process employed by the U.S. Minerals Management Service and other regulatory agencies,” said Winter.

The committee was convened at the request of Secretary of the Interior Ken Salazar to conduct an independent and science-based investigation into the root causes of the Deepwater Horizon oil spill that amounted to 4.9 million barrels before the well was capped on July 19. The oil spread across a vast expanse of the gulf, causing widespread fisheries closures and fouling hundreds of miles of shoreline and wetlands.

Eleven crew members died and 17 others were hurt in the initial explosion April 20 at a site 40 miles southeast of the Mississippi Delta.

“It may not be possible to definitively establish which mechanisms caused the blowout and explosion, given the deaths of 11 witnesses on board, the loss of the oil rig and important records, and the difficulty in obtaining reliable forensics information from the Macondo well,” the committee says in its peer-reviewed report

Nevertheless, the committee said it has been able to develop “a good understanding” of a number of key factors and decisions that may have contributed to the blowout of the well.”

On the issue of safety vs saving money, the committee’s report contradicts last week’s assertions of the presidential commission investigating the disaster that there is, “No evidence at this time to suggest that there was a conscious decision to sacrifice safety concerns to save money.”

Citing testimony given at the Marine Board of Inquiry hearing into the disaster on July 22 by BP Wells Team Leader John Guide, the committee states, “many of the pivotal choices made for the drilling operation and temporary abandonment of the well were likely to result in less cost and less time relative to other options…”

Decisions that contributed to the accident began with continuing abandonment operations at the Macondo site despite several tests that indicated that the cement put in place after the installation of a long-string production casing was not an effective barrier to prevent gases from entering the well, the committee said.

“The decision to accept the test results as satisfactory without review by adequately trained shore-based engineering or management personnel suggests a lack of discipline and clearly defined responsibilities,” the committee reported.

“In addition, several clear failures in monitoring of the well appear to have contributed to its blowout; available data show hydrocarbons entered the well undetected for almost an hour before the first explosion.”

“Timely and aggressive action to control the well was not taken, and for unknown reasons, hydrocarbons were funneled through equipment that vented them directly above the rig floor rather than overboard. These conditions made ignition “most likely,” the report says.

Finally, the blowout preventer did not seal the well once activated.

Of particular concern, the committee said, is the “lack of a systems approach to integrate the multiple factors impacting well safety, to monitor the overall margins of safety, and to assess various decisions from a well integrity and safety perspective.”

The report also notes that a previous loss of hydrocarbon circulation in the Macondo well on March 8, more than a month before the accident, presented an opportunity to take actions to mitigate future risks.

The committee pointed to three questionable decisions that were made about the cementing process prior to the accident:

• attempting to cement across multiple hydrocarbon and brine zones in the deepest part of the well in a single operational step, making a hydraulic fracture in a low-pressure zone more likely

• using a long-string production casing instead of a liner over the uncased section of the well

• deciding that only six centralizers were needed to ensure an even spacing between the formation rock and the casing, even though modeling results suggested that more centralizers would have been necessary
The committee said the type and volume of cement used to prepare for well abandonment and the time provided for the cement to cure may also have impacted the well’s integrity.
The federal government came in for a share of blame in the committee’s report, particularly the Minerals Management Service, MMS, which the committee found “did not have a formal training and certification program for its inspectors.” MMS was responsible for review and approval of permits and plan for the drilling and completion of the Macondo well.

Federal agencies lacked information about what other agencies were doing, the committee found.

As the flag state of the Deepwater Horizon, the Republic of the Marshall Islands was responsible for conducting safety inspections and surveys and monitoring compliance with national and international safety standards.

The American Bureau of Shipping and Det Norske Veritas, two classification societies, conducted surveys and audits required for issuance of certificates on behalf of the Marshall Islands.

The U.S. Coast Guard had responsibility for ensuring the Deepwater Horizon met the safety requirements for rigs operating in the U.S. Outer Continental Shelf Region.

“From testimony,” wrote Winter in the committee’s report, “it appears that the various organizations mentioned above sometimes were not certain of the oversight duties actually being carried out by other organizations.”

The testimony he cites was given at the Marine Board of Inquiry hearing into the incident on May 12, by Capt. Thomas Heinan, deputy commissioner maritime affairs, Marshall Islands; and the May 26 testimony of John Forsyth, assistant chief surveyor, American Bureau of Shipping.

BP and the contractor companies offered no immediate comment on the interim report.

For its final report, due in the summer of 2011, the committee will examine ways to establish practices and standards to foster a culture of safety and methods to ensure that schedule and cost decisions do not compromise safety.

The committee will assess the extent to which there are gaps, redundancies, and uncertainties in responsibilities of multiple agencies and professional societies overseeing deepwater drilling operations, and it will consider the merits of an independent technical review to provide operation checks and balances by enforcing standards and reviewing deviations.

The Macondo well’s blowout preventer was only recently recovered and is undergoing forensic analyses. The committee will evaluate possible causes for the failure of the blowout preventer once key data are made available.

Secretary Salazar said today that the committee’s “independent, science-based analysis of what went wrong in the lead up to the blowout will help guide our continuing efforts to raise the bar for safety and oversight of offshore oil and gas operations, and will be of assistance to other ongoing investigations.”

Michael Bromwich, director of the department’s Bureau of Ocean Management, Regulation and Enforcement, the agency that took over the functions of the discredited and disbanded Minerals Management Service, said,

The work of the NAE and NRC team “will help guide our continuing efforts to strengthen standards and oversight and underscores the importance of our ongoing efforts to build a strong and independent agency with the resources, training, and expertise to provide aggressive oversight of offshore oil and gas operations to ensure that offshore energy production is conducted “in a manner that protects human life and the environment.”

NATIONAL ACADEMY OF ENGINEERING
NATIONAL RESEARCH COUNCIL

Committee on the Analysis of Causes of the Deepwater Horizon Explosion and Oil Spill to Identify Measures to Prevent Similar Accidents in the Future

Donald C. Winter (chair)
Former Secretary of the Navy, and
Professor of Engineering Practice
Department of Naval Architecture and Marine Engineering
University of Michigan, Ann Arbor

Paul M. Bommer
Senior Lecturer
Department of Petroleum and Geosystems Engineering
University of Texas, Austin

Chryssostomos Chryssostomidis
Doherty Professor of Ocean Science and Engineering
Massachusetts Institute of Technology, Cambridge

David E. Daniel
President
University of Texas, Dallas

Thomas J. Eccles
Rear Admiral, and
Chief Engineer and Deputy Commander for Naval Systems Engineering
U.S. Navy, Washington, D.C.

Edmund P. Giambastiani Jr.
Private Consultant and retired U.S. Navy Admiral
Warwick, Maryland

David A. Hofmann
Professor of Organizational Behavior
Kenan-Flager Business School
University of North Carolina, Chapel Hill

Roger L. McCarthy
Private Engineering Consultant
Palo Alto, California

Najmedin Meshkati
Professor of Engineering
Viterbi School of Engineering
University of Southern California, Los Angeles

Keith K. Millheim
Director and Owner
Strategic Worldwide, LLC
The Woodlands, Texas

Elisabeth Pate-Cornell
Burt and Deedee McMurty Professor and Chair
Department of Management Science and Engineering
Stanford University, California

Robert F. Sawyer
Class of 1935 Professor of Energy, Emeritus
Department of Mechanical Engineering
University of California, Berkeley

Jocelyn E. Scott
Chief Engineer and Vice President of Engineering, Facilities, and Real Estate
DuPont
Wilmington, Delaware

Arnold F. Stancell
Turner Professor of Chemical Engineering, Emeritus
Georgia Institute of Technology, and
Vice President of Mobil Oil (retired)
Greenwich, Connecticut

Mark D. Zoback
Benjamin M. Page Professor of Earth Science, and
Professor
Department of Geophysics
Stanford University
Stanford, California

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